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Showing posts from September, 2019
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Gantt Chart for ME195-A Half-Scale Team For our timeline, the next two weeks will be crucial (9/28/19-10/9/19) as each of us would be working on the CAD prototypes for each of the respective mechanical systems. After that, we would be doing inventory checks and basic testings on the motors, Arduino boards and gears as carried on by previous Half-Scale teams. After that, we would be implementing our CAD designs and constructing our sectional model for each of the systems which, if successful, would be carried into ME195-B and used be used as our prototypes.
We have conducted trial runs of the bogie system to analyze its functionality and have found several problems with the gearing, switching mechanism and the track layout. In order to correct these issues, we have decided to redesign the switching mechanism and add additional gears to the drive system as it tends to separate from the teeth of the drive motor. The switching mechanism is only partially functional and must also be redesigned due to structural weaknesses in the pin that holds the rocker, which lowers the factor of safety substantially. As the the Half-scale team, we have chosen to redesign the switching mechanism by removing the 'rocker style' arm that is currently being used and replacing it with a 'T-shaped' bar with a wheel attached. By these redesigns along with modifications to the track, we will be able to navigate the track with full functionality.